
The
easiest tweak is a short length of soft automotive vacuum line slit
lengthwise, then taped to the cocking lever. Makes cocking much more
comfortable.

I
am not sure how this happened on an otherwise good design. Perhaps they
used a larger screw later in production. On my pistol, the screw
threads extend into the bolt groove, causing the bolt to drag which causes loss of velocity and accuracy. It also can damage
the bolts. I used a round
needle file to bring the threads down flush with the groove. However,
this made scratches in the black finish. Might be better to remove the
screw to do that.
Accuracy
You can increase accuracy by testing the bolts in the groove. Press
down on the front of the bolt. If there is a gap, then turn the bolt
over and try again. If it lays against the groove, use an indelible
marking pen to make a mark on the underside of the bolt tip so that you
can always get the bolt inserted so that the nose does not stick up.
While
we are checking bolts, make sure the tip and "feathers" are firmly
attached. I use a small drop of Gorilla Glue, or other polyurethane
glue. It expands as it sets.
When
you install the bow into the stock, measure the distance from the tips
on each side to make sure the bow is centered. I am not sure if it was
recommended in the instructions, but I have a couple of layers of
electrical tape wrapped around the bow where it is clamped into the
stock. A scrap of leather would be even better.
With
the bow strung but not cocked, the string should form a 90° angle with
the sides of the pistol. If it is not square and loosening and re
tightening the bow retaining screw does not correct it, put one or two
strips of paper under one side of the bow where it contacts the stock.

You
can gain a slight increase in velocity by bending this spring upward to
reduce drag. If you bend it too much, accuracy will suffer. Simply bend
it back some if you need to.

This may be your
best bet for accuracy improvement. Remove both the front and rear
sights. If the bow is strung, cock it and
put the safety
on.
Wrap a small piece of 600 grit 'wet or dry' silicon carbide paper
around
one of the aluminum bolt shafts or something else 1/4" in diameter
(like a drill bit).
Lightly sand the edges of the bolt groove. This
only takes a few seconds and you should be able to feel the groove
edges where it contacts the bolt getting smoother. Do the full groove
length.
After doing
this I put 4 shots in the same hole at 15 feet.Broadhead
bolt, or quarrel (4-sided head)
A
length of fiberglass arrow can be used to make broadhead bolts
for
your crossbow pistol. The shaft must be longer so that the broadhead
sticks out in front of the pistol.
Do not use a
good saw to cut the fiberglass. I guarantee it will be
ruined. Or use an abrasive cutoff wheel on the hand grinder.
Don't breath
the dust.
Fishing
Crossbow

Like
to fish? These barbed bolts are available on eBay.
Folding
Shoulder Stock
This
folding stock was made from 3/16 steel rod and two heavy solder type
copper terminal lugs meant for electrical work. The lugs can be
epoxied or soldered on. The 90° bend at the butt was made by
heating the rod
with a pencil tip propane torch, then bending in a vise. Note that
having the stock folded does not interfere with using it as a pistol.

Open, it adds
greatly to stability and makes hitting small targets easy.
UPDATE
I filed the underside of the screw head and soldered it to
the
copper lug. That prevents the screw from turning when you adjust the
wing nut.
An
operation analysisI
experienced string jump-over a few times, especially on short bolts.
The point where the string contacts the rear of the bolt resembles this:

It
may be possible to file the rear of the channel to center the string at
the center of the bolt. I made the channel slope in the area 1.5 inches
from the rear where it is slotted to a bit over 1/4" wide; there is no
support for the bolt in this area. This made the string contact the
bolt rear at mid height.
Safety too
stiff?On my pistol, it took a great effort to
put the safety on, and a Herculean effort to side it off.
Make
modification at your own risk!Removing
the sheet metal covers reveals the safety bolt. Be careful not to lose
the shiny metal tube, two small springs, or detent.
Safety boltThe
red arrows point to the two grooves that engage the spring loaded
detent.
Safety DetentI
used sand paper to change the shape as above. If you try this, only
remove a little material at a time, then try it for fit. Your thumb
over the detent will (hopefully) prevent it from flying out as you fit
it.
Now I can flip it back and forth using only my
thumb instead of both hands.
LubricationI
tried bees wax as recommended for full size crossbows. It created way
too much drag. Chapstick worked better for me. Squeezing the two
cocking prongs gently together showed that the cocking rod needs lube
too. A little chapstick on the sides where the rod contacts the frame
reduced the amount of effort to cock it greatly.
Repeating
Crossbow Pistol
Okay,
I had to do it. Not shown is the magazine follower. It holds 6
shortened bolts in this configuration (above). Several problems were
solved doing this: string pop up that hops over the bolt causing
misfires. String oscillation that robs power. The stack prevents the
rear of the bolt from dropping which results in wild shots.
Short
bolts have more initial velocity which gives greater penetration and
less drop at a distance. But there is a problem. Shortening the bolts
exaggerates flaws in manufacture and many may not fly straight.
NEW
I
wanted to try real feathers in the crossbow pistol, but needed some way
to align the feathers accurately. I came up with this idea.

A
scrap or plywood was chosen longer than the bolts. Four long grooves
were cut using the table saw. I got lucky the first time and the bolts
fit perfectly with the bottom of the bolt barely touching the bottom of
the groove. If it had not, then I would simply sand the top surface.
The red area is beveled slightly to make room for glue, and the
finished fletching tool coated with floor wax to prevent glue from
sticking. The weight is about 4" long of oak. Use what scrap you have
on hand.
After I made a few bolts with feathers, it occurred to
me that this tool could also be helpful for making the broad
heads. Now it is easy to get perfect alignment of the razor blade
in the slot in the bolt tip.
In tests, the feathered bolts do
penetrate better than the plastic fins on the factory bolts. I assume
this is because the velocity is higher with the reduction in weight at
the rear.

Plans for this gem are now for sale on
this page cheap. It uses standard bolts.